More fixing on the Fairlane today. The oil filter has been leaking so I changed it out and that worked for a few miles but it started dripping again. I took it off and took off the adapter that changes a cannister type to a spin-on and checked it all over. It looked good to me so I cleaned it up and reinstalled it and the filter, and I magically fixed it. I don't know how. [can I write about magic here]?
Anyhow, I've been trying to find out why I don't have my overdrive anymore, and today I took out my kick-down switch, [from a really horrible place on the front of the toeboard], and checked it. When I was installing my motor I must have bumped the switch and bent one electrical spade so it touched another one. Did I mention that it was the job from heck. There was the exhaust pipe, the clutch linkage, the shifter rails, the belhousing, the speedometer cable, and the emergency brake cable all competing with my hand in there.